In the early days of the museum, the only interior space was inside the trolleys. So, the cars that were not used for service (because they were unfit to operate, missing components, etc) became storehouses for other smaller materials that we acquired. Unfortunately, some of those materials have considerable weight to them which will stress the cars body. Connecticut Company 0309 (Fair Haven & Westville 154) is one of them that was loaded with overhead parts (insulators, bolts, etc). On Saturday, David Coppola helped me unload the materials stored inside the car onto shelf space inside the Visitor Center Relay Room. The only items left in the car now are parts to the car.
Inside the Visitor Center, Galen Semprebon, Brian Semprebon, and Matty Doane were working on scraping the exterior paint on Montreal Tramways 2056 (Springfield Street Railway 575). The car needs a new coat of paint and the plan is to return the car to Springfield, MA colors. While this will not be a complete restoration at the current time, it is a start in the direction to returning the car to its local history. In order to complete the restoration of the car, it will need an end reduction, because when the car was sold to Montreal Tramways, they extended the ends of the car and reconfigured the operators compartment.
Outside, John Pelletier, with the help of Matty, Galen, and I, was working on the repairs to the operating fleet. The bent pole on Connecticut Company 1326 was straightened and the car was returned to service. The broken retriever on Illinois Terminal 451 was replaced by a rebuilt one found in the Parts Storage Room. The repairs to Montreal Tramways 2600 took a bit longer. There was a squealing noise coming from the number 3 axle. We checked the packing and oiled the Journal Boxes. The temperature of the number 3 axle journals were slightly elevated. When we took it out for a test, the noise was still there. We finally figured out that it was the cause of the armature bearing. The waste in the bearing was failing and not properly wicking the oil. Once we repacked the bearing, the noise subsided. The armature support bearing for the fourth motor has been freed and should be repaired in the next few weeks. Once that is done, the car will be jacked and the motor will be reinstalled in the trucks.
We had another busy night of Winterfest Operation Saturday night with 5 cars out on the main line at one point. With that many cars, there is a slight bottleneck at Hancock Passing Siding. The track with three cars needs to pass through the siding before the track with two cars on it can proceed because the siding is only two cars long.
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